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1979 Ford LTD, barn find FTW

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    #61
    How many valve cover bolts does that have? Should post up some more pics!
    sigpic


    - 1990 Ford LTD Crown Victoria P72 - the street boat - 5.0 liter EFI - Ported HO intake/TB, 90 TC shroud/overflow, Aero airbox/zip tube, Cobra camshaft, 19lb injectors, dual exhaust w/ Magnaflows, Cat/Smog & AC delete, 3G alternator, MOOG chassis parts & KYB cop shocks, 215/70r/15s on 95-97 Merc rims

    - 2007 Ford Escape XLT - soccer mom lifted station wagon - 3.0 Duratec, auto, rear converter delete w/ Magnaflow dual exhaust

    - 2008 Mercury Grand Marquis Ultimate Edition - Daily driver - 4.6 2 valve Mod motor, 4R75E, 2.73s. Bone stock

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      #62
      oOo it even has the original old school awesome air cleaner! What modifications have to be made to fit that in the LTD? What transmission is that?? This could be very interesting! should make some power too, especially if you went 4BBL! Even the 2bbl made awesome power
      Last edited by Brown_Muscle; 12-18-2011, 04:14 PM.
      -Phil

      sigpic

      +1982 Ford LTD-S Police Car. Built 351w, Trickflow 11R 190 Heads, Holley Sniper EFI, RPM Intake+ Hyperspark dizzy, WR-AOD, Full exhaust headers to tails. 3.27 Trac-Lok Rear. Aluminum Police Driveshaft. Speedway Springs+Bilstein Shocks, Intermediate Brakes, HPP Steering Box.

      +2003 Acura CL Type S 6-speed

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        #63
        Originally posted by 1990LTD View Post
        How many valve cover bolts does that have?
        8 bolts for Cleveland vs 6 bolts for Windsor
        Last edited by Mercracer; 12-18-2011, 04:23 PM.

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          #64
          Originally posted by flyb0t View Post
          On an unrelated note, can anyone explain why my Grand Marquis is misfiring/bucking at speed? Literally everything on the motor has been replaced once (or twice) recently, and yet nothing is resolving this misfire/bucking idle/bucking-jerking while driving. Only things that haven't been replaced are the timing chain (which we checked and think it's still okay) and the TFI module, which we tested and verified working.
          Vacuum leak is #1 thing to check...

          Comment


            #65
            Originally posted by Brown_Muscle View Post
            oOo it even has the original old school awesome air cleaner! What modifications have to be made to fit that in the LTD? What transmission is that?? This could be very interesting! should make some power too, especially if you went 4BBL! Even the 2bbl made awesome power
            The tranny bolted to it is a C4, which since there is already one in the car doesn't make a ton of difference. The modifications that I can tell so far is that we would have to swap the oil pan and & pump (rear sump vs. front sump), delete a bunch of the emissions stuff, and figure some fancy way of making or modifying a set of headers to sneak back through to the rest of the exhaust. Early estimates from web results place that motor at making around 250HP as it sits, and with only a handful of modifications (intake, etc), making gobs of power. Finding a set of 4bbl heads would be good as well, but for now, that's plenty of power, as long as it's in the car.


            As for the Mercury, Mercracer, I'll have to check for vacuum leaks. Weird thing is, it will will start okay, and idle okay, but then as soon as it starts to get moving, it starts to bork up. Is this symptomatic of a vac leak? Or is it something wiring related?
            1984 Mercury Grand Marquis LS (Daily Driver)
            1979 Ford LTD-S (Project)

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              #66
              Originally posted by Mercracer View Post
              8 bolts for Cleveland vs 6 bolts for Windsor


              ...which is why I was asking. I can see 6 but I think snow is covering up the other two. If there are no other two, it's a Windsor.


              They don't look like they're in the same arrangement as a Windsor, though (3 along the bottom.)
              Last edited by 1990LTD; 12-18-2011, 08:03 PM.
              sigpic


              - 1990 Ford LTD Crown Victoria P72 - the street boat - 5.0 liter EFI - Ported HO intake/TB, 90 TC shroud/overflow, Aero airbox/zip tube, Cobra camshaft, 19lb injectors, dual exhaust w/ Magnaflows, Cat/Smog & AC delete, 3G alternator, MOOG chassis parts & KYB cop shocks, 215/70r/15s on 95-97 Merc rims

              - 2007 Ford Escape XLT - soccer mom lifted station wagon - 3.0 Duratec, auto, rear converter delete w/ Magnaflow dual exhaust

              - 2008 Mercury Grand Marquis Ultimate Edition - Daily driver - 4.6 2 valve Mod motor, 4R75E, 2.73s. Bone stock

              Comment


                #67
                Originally posted by flyb0t View Post
                As for the Mercury, Mercracer, I'll have to check for vacuum leaks. Weird thing is, it will will start okay, and idle okay, but then as soon as it starts to get moving, it starts to bork up. Is this symptomatic of a vac leak? Or is it something wiring related?
                it could also be the PIP in the distributor going out. It could also be the noise suppressor capacitor on the coil going out. if enough noise gets into the EFI's thought process, all manner of crap will happen.

                Only two things are infinite, the universe and human stupidity, and I'm not sure about the former. -- Albert Einstein
                rides: 93 Crown Vic LX (The Red Velvet Cake), 2000 Crown Vic base model (Sandy), 2003 Expedition (the vacation beast)

                Originally posted by gadget73
                ... and it should all work like magic and unicorns and stuff.

                Originally posted by dmccaig
                Overhead, some poor bastards are flying in airplanes.

                Comment


                  #68
                  Originally posted by 1990LTD View Post
                  ...which is why I was asking. I can see 6 but I think snow is covering up the other two. If there are no other two, it's a Windsor.


                  They don't look like they're in the same arrangement as a Windsor, though (3 along the bottom.)
                  I will bet you paychecks that it is a 335 series motor....


                  If you look close you will see that there are 4 along the bottom and 4 along the top..... I have been working on these things for over 25 years...
                  Last edited by Mercracer; 12-18-2011, 10:51 PM.

                  Comment


                    #69
                    Originally posted by slymer View Post
                    it could also be the PIP in the distributor going out. It could also be the noise suppressor capacitor on the coil going out. if enough noise gets into the EFI's thought process, all manner of crap will happen.
                    will the suppressor dieing out really fuck with the EEC? iv never heard this before, very interesting though. wonder what would happen if you unplugged it, just to verify lol

                    1981 Mercury Marquis Brougham 2-Door 302/ 5-speed -special blend (GMGT)
                    1987 Lincoln Mark VII 5-speed (Errand runner)
                    1989 Mercury Grand Marquis (Base Runner)
                    2007 Lincoln Town Car Signature Limited (Hustlyn)
                    2011 Ford Crown Victoria Police Interceptor (Down with O.P.P)

                    Comment


                      #70
                      Originally posted by slymer View Post
                      it could also be the PIP in the distributor going out. It could also be the noise suppressor capacitor on the coil going out. if enough noise gets into the EFI's thought process, all manner of crap will happen.
                      Already replaced the entire dizzy. Replaced the cap and rotor (twice). Ignition coil, TFI module, Thermostat, Timing Chain are about the only things that haven't been changed.

                      As for all the debate on whether or not it's a cleveland, sorry I didn't get the best picture, but I did count as soon as I saw it and there were 8 bolts on the cover. I will take more pictures as soon as I can.
                      1984 Mercury Grand Marquis LS (Daily Driver)
                      1979 Ford LTD-S (Project)

                      Comment


                        #71
                        Originally posted by Mercracer View Post
                        I will bet you paychecks that it is a 335 series motor....


                        If you look close you will see that there are 4 along the bottom and 4 along the top..... I have been working on these things for over 25 years...

                        I wouldn't take that bet since I looked closer at the arrangement of the bolts.
                        sigpic


                        - 1990 Ford LTD Crown Victoria P72 - the street boat - 5.0 liter EFI - Ported HO intake/TB, 90 TC shroud/overflow, Aero airbox/zip tube, Cobra camshaft, 19lb injectors, dual exhaust w/ Magnaflows, Cat/Smog & AC delete, 3G alternator, MOOG chassis parts & KYB cop shocks, 215/70r/15s on 95-97 Merc rims

                        - 2007 Ford Escape XLT - soccer mom lifted station wagon - 3.0 Duratec, auto, rear converter delete w/ Magnaflow dual exhaust

                        - 2008 Mercury Grand Marquis Ultimate Edition - Daily driver - 4.6 2 valve Mod motor, 4R75E, 2.73s. Bone stock

                        Comment


                          #72
                          Hey if you want I coud come down and help ya out if you wish
                          89 townie, mild exhuast up grades, soon to have loud ass stereo....

                          Comment


                            #73
                            Originally posted by marquisman View Post
                            will the suppressor dieing out really fuck with the EEC? iv never heard this before, very interesting though. wonder what would happen if you unplugged it, just to verify lol
                            yes, it can if it goes out completely. You would however probably notice this on a stock radio because you would have the RPM based humming. Some newer aftermarket radios have filters for that noise. Older EEC is more susceptible to it than some of the newer stuff, but if the noise is larger than the hysteresis of the signals (the difference between on and off in a digital signal) it will create all manner of f'd up signals for the EEC to try to contend with.

                            Has the TPS been checked? Maybe it's turned digital instead of analog.

                            Only two things are infinite, the universe and human stupidity, and I'm not sure about the former. -- Albert Einstein
                            rides: 93 Crown Vic LX (The Red Velvet Cake), 2000 Crown Vic base model (Sandy), 2003 Expedition (the vacation beast)

                            Originally posted by gadget73
                            ... and it should all work like magic and unicorns and stuff.

                            Originally posted by dmccaig
                            Overhead, some poor bastards are flying in airplanes.

                            Comment


                              #74
                              That motor is obviously a cleveland since the valve cover is a perfect rectangle. On a windsor the ends of the valve covers are diagonal and they're longer on the bottom and shorter on the top.

                              Comment


                                #75
                                Originally posted by slymer View Post
                                yes, it can if it goes out completely. You would however probably notice this on a stock radio because you would have the RPM based humming. Some newer aftermarket radios have filters for that noise. Older EEC is more susceptible to it than some of the newer stuff, but if the noise is larger than the hysteresis of the signals (the difference between on and off in a digital signal) it will create all manner of f'd up signals for the EEC to try to contend with.

                                Has the TPS been checked? Maybe it's turned digital instead of analog.
                                TPS has been checked, verified bad, and replaced. Still no resolution. There's no vacuum problem, we checked for that today. Found it runs better with the SPOUT connector disconnected, though it still has a hitch and a roughish idle, but nowhere near as bad as when the computer is enabled. I'm plum out of ideas, short of maybe checking back into the EGR, though we cleaned out and replaced all those components some months ago.

                                As for the motor, I have a few more pictures I can put up directly. We found it doesn't roll over completely, however it does move. Thanks to the good fortune of all the snow (!) melting off up here, we may be able to put some progress forward.

                                And some progress on the LTD itself, with what some body work still needing done.
                                1984 Mercury Grand Marquis LS (Daily Driver)
                                1979 Ford LTD-S (Project)

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